No photos this time around, but I did a flush, intake cleaning and change on my 2019 Kia sportage with 105k miles, initially filled with dealer oil 5W20 when we got it last month. Then, over the last 6k miles ives topped off with what I had, which was about 3 qts of QS Euro 5W40 and then probably another 4qts of Valvoline Restore and Protect 5W30.
I started by putting 1 bottle of Redline in a nearly empty tank and filled with 93 TopTier fuel from Citgo. (side note: I had previously ran Royal Purple's Max Clean with a full tank of 93 TT and their max atomizer back to back with 93 TT in half tanks each)
About half a tank and a day later, this morning I added 1 can of BG EPR and ran that through for about 15 minutes at 1200 rpm.
Next, without draining the sump, I used CRC for 1 second bursts at 2000 rpm into the throttle body until empty.
While it was heat soaking, I drained the oil and filled with 5qts of Valvoline Restore and Protect 5W30, and replaced the dealer oil filter (forgot the brand, it was a generic looking white canister) with a Fram 10k filter. I let it soak some more, about 30 minutes, until it was time to test drive it. I also replaced the PCV valve.
After about 40 miles since the CRC and oil flush/change, I think the rough idle has finally been resolved. Will be interesting to see how this effects the oil consumption too.
Doing my next change at 110k miles (about a 5k oci).
I started by putting 1 bottle of Redline in a nearly empty tank and filled with 93 TopTier fuel from Citgo. (side note: I had previously ran Royal Purple's Max Clean with a full tank of 93 TT and their max atomizer back to back with 93 TT in half tanks each)
About half a tank and a day later, this morning I added 1 can of BG EPR and ran that through for about 15 minutes at 1200 rpm.
Next, without draining the sump, I used CRC for 1 second bursts at 2000 rpm into the throttle body until empty.
While it was heat soaking, I drained the oil and filled with 5qts of Valvoline Restore and Protect 5W30, and replaced the dealer oil filter (forgot the brand, it was a generic looking white canister) with a Fram 10k filter. I let it soak some more, about 30 minutes, until it was time to test drive it. I also replaced the PCV valve.
After about 40 miles since the CRC and oil flush/change, I think the rough idle has finally been resolved. Will be interesting to see how this effects the oil consumption too.
Doing my next change at 110k miles (about a 5k oci).