What are you working on today?

Worked on it more today. I got the rubber floor in but when I went to tighten the seat belt bolt down it would only go so far and then no more. I backed it out and then it would only go so far and now it just spins in place and won't come out.

My fiancé's dad came over and he cut off the top of the bolt and we tried putting a jack on the bolt from underneath the truck to put pressure on it and it still just spins in place and basically is stuck in one spot. Now it's going to have to be drilled out.

I don't have any drill bits that will drill out hardened bolts. Anyone have any suggestions on what kind of drill bits to get?

As far as the Torx size, I don't know. In this case, it wouldn't have mattered because this bolt wasn't going to come out with any torx bit. I'm tired of messing with this thing and it's not even my truck. It never fails. Any time I work on something these days, something always goes wrong.
Personally I'd buy several inexpensive unibits. If they cut, abuse them and replace if one burns up. But if it's spinning now it's going to try to spin while drilling

How are you spinning the bolt if you cut the head off?
 
Putting in simple 12" square grey pavers along side the drive just to the front of my truck. I park close to the edge to make room on the other side for the wife's vehicle and so our doors do not hit each other when open. The grass would not grow due to shade trees so I figured simple pavers would work. Plus, when I take my daughter on rides her wheel chair will no longer be in the dirt. I'm going only 3 pavers wide and just down far enough so I can get onto the main driveway with her wheel chair.

I had 811 come out to mark utilities but even though I was careful I still nicked the internet line. So that will be a nice fix it bill from Spectrum. Live and learn.

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Get some 3M underground spicing tape and cover it up. 3M C130
 
Going to be a stormy day so maybe do some of those rainy day jobs? More than likely watch it rain and check out my drainage projects.
 
Personally I'd buy several inexpensive unibits. If they cut, abuse them and replace if one burns up. But if it's spinning now it's going to try to spin while drilling

How are you spinning the bolt if you cut the head off?
Vice grips. Yes, it's going to be difficult to drill it out. Someone will have to hold the remains of the bolt from the bottom as someone drills from the top. It's definitely a mess.
 
Well, I finally got the bolt out. I used a Carbide drill bit and cut off some of the bolt that was under the truck with a sawzall and metal blade. I also used a punch and hammer to finally drive the rest of it out. It took me about 3 hours. Tomorrow I will have to go buy a bolt and nut to replace it and then put the rest of the interior back in.
 
Moved a Subaru engine from the garage to the backyard onto a pallet. Almost sold it but fella lowballed.
 

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Worked on my brother's IDI bullnose Ford. He was complaining that it seemed like it was leaking more transmission fluid that usual... I had him start it up for me and found both steel cooling lines had been rubbing against a bracket for 30 plus years till they both were worn down to the point of pin hole leaks. Amazing that they both rubbed through at the same time. I pulled them off and cut them off at the leaks and added extra rubber line to keep him on the road until we can get new steel lines. Since there was no barb on the lines, I double clamped everything, but I'm nervous about him running it out of oil.
 
Finished up the install of a front receiver and homeowner Snowbear plow on an '08 F150. The plow actually comes with turnbuckle braces on either side of the receiver which I thought was a great idea, but they're designed for a hitch where the receiver tube bisects the cross beam.

The Curt is built with the receiver tube below the cross beam:
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So I added rectangle tube on either side:
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Turnbuckle braces now function:
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Installed an aluminum oil filter housing and cooler in my niece’s Grand Caravan. Home stretch before she can use it. I want it to be functionally near perfection since she carts my youngest nephew around in it.

I have done this enough that it’s muscle memory now, and I had it in place by lunchtime. And I started late.

Put in coils and plugs since I had easy access. Those plugs that were in there were barely hanging on, from how they looked. 😦

It ran like crud and it was initially due to the intake hose being slightly off. 🫤

Put it all back, and it gradually improved. I suspect I may have to disconnect the battery for a bit to get the throttle body to reset.

It has a steering angle sensor issue, and I suspect it’s related to the all new control arms, etc., that were installed. The alignment is off a touch, and with these they seem to be sensitive to a crooked steering wheel. Alignment scheduled for Tuesday.

Pics attached…
 

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Friday I had a neighbor bring their son's Tahoe by the house for some routine maintenance. Oil change, tire rotation, brake inspection. Ended up replacing the front pads.

Saturday I did some cleaning up around the house.
 
Oil change, followed by draining 2L CVT and refilling. Started on the tire rotation, taking all the brakes apart and applying anti seize. Both rear rims froze in place, along with both rotors. Freed up now, almost done, but dinner takes priority.
 
Oil change on a 2016 Fusion 2.0 EB
He went 1 year (to the day) and ~10k on Motorcraft 5w30 😭
It looked dark, thin, and was at least 1qt low 😳
This time, he got Total MC3 5w30/910s and a 6 month interval

Oil change on the 2001 Villager (62k), it's gone 205 miles since last year, so the oil drained was clean
4qts Total SL 5w30/Bosch filter

Dad's work van got the H9 mod for low beams instead of the bogus LEDs that were loosely installed
Need to get some H11s for the high beams, washer fluid, general fluid top off
Then I pulled the cabin filter
I believe by the date code and manufacturer, it is the factory part
2011 Grand Caravan with 220k+ on it 😳
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I pulled many acorns out of the blower motor, probably gonna have to drop it to clean it out 🤮
He's getting new wiper blades and CAF when the RockAuto delivery comes in the week
 
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I got to be a hero with the wife by fixing our LG front load washer. The drum suddenly had runout and it was melting the rubber door seal as it rubbed while spinning. I found a YT vid where he started off thinking bearings but it was the spider arm:


So I had ordered a new spider arm, bearing and seal kit, shock absorbers and door seal. Total was around $250 so it was a more affordable proposition than a new washer ;)

The wife thought I was crazy to drag the machine to the shop but I knew there would otherwise be a dozen trips back and forth for tools. The older I get, I want to work smarter, not harder -- even if smarter takes longer. I also got the machine on my hydraulic cart so I could adjust the height --- no squatting to work at floor level!!
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Being a tool junkie paid off as a couple years ago I bought to tool for the door seal spring on Amazon Warehouse Deals
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I had to disconnect nine plugs just to get the control panel off. Pretty sure you can find EFI harnesses with fewer! Rant: appliances don't need to be this complicated
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Once I finally got to the metal drum (which is basically 99% disassembly of the ENTIRE machine) I was a bit confused because my arm wasn't cracked and the bearings felt great. But upon closer inspection the arm was adding its own speed holes. It was also so tight in the drum I couldn't pry it out so I cut one arm to release the tension. Fortunately I stock aluminum-rated cutoff wheels:
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New vs old, note the air gaps in the old were solid Al once upon a time:
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