Thank you, they look nice 

WHOA. I don't even have words.Just a few photos for today. I'm glad this broke while I was only moving around on the driveway. Sigh.
I was a bit agast too. it was in neutral at the time and was in a safe situation but was still very much puckered. I pushed the truck back up the driveway with my other truck.WHOA. I don't even have words.
I was a bit agast too. it was in neutral at the time and was in a safe situation but was still very much puckered. I pushed the truck back up the driveway with my other truck.
I have a brand new shift tower and lever coming tomorrow.![]()
Just a few photos for today. I'm glad this broke while I was only moving around on the driveway. Sigh.
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A few updates from the past few weeks. New cab lights soldered in. The old ones were wire twisted on. Sigh.
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I sent off the fuse box and it should be back this upcoming week. Swapping a few junkyard FCMs didnt help. The circuit board was definitely kaput where all the blinking/hazard stuff happens (lower left). I also asked the repair folks to replace the 3 non serviceable tow light relays (upper right), and have a look at whatever is going on in the center left with the holes.
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Out with the old shifter, my god it was disgusting.
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In with a new shifter. It feels much, much better.
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Onto evaluating the 4wd system, starting with the front differential. Suctioned out the front fluid, it didnt look terrible. In went about 1.5 quarts of Mobil 1 75w90. I am holding further to see if the front axle seals leak and will revisit with a new differential gasket.
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And onto the biggest bummer, the transfer case fluid was probably one of the top 5 worst drain's i've ever done. Now I know why the front driveshaft was removed. I will attempt a rebuild later. In went 1 quart of Supertech ATF+4, 1 quart Valvoline ATF+4.
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Transfer case gunk.
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This used to be ATF+4. Welcoming any comments on their experience with draining a transfer case and seeing a horror show like this.
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I have seen some glaring omissions on Carfax reportsI LOVE carfax.
the beauty of the Ram Cummins is the whole truck will self destruct around an engine that will never quit if you keep oil in it..I was a bit agast too. it was in neutral at the time and was in a safe situation but was still very much puckered. I pushed the truck back up the driveway with my other truck.
I have a brand new shift tower and lever coming tomorrow.![]()
That's a shame why get rid of it if it still works .I've been on the hunt for a replacement truck. I am near ready for bigger projects that require more towing capability. My Silverado will be sold to a family friend later this year. I won a 2003 Ram 3500 6 speed 4x4 manual at auction. She is entirely clapped out inside and somewhat outside. AC? Heat? What AC controls? Those are now options as there is a gaping hole where one once was. Stereo works with a USB port. The driver seat was gross, so I sat on a beach towel. The fender and hood do not match the rest of the body, and the tailgate which does not open is red. Its patriotic. The carfax showed no wrecks, so those white parts happened for whatever reason my imagination will think up. The odometer works, but carfax kindly outlined that its not original. I need to do some math but its probably in the 350k+ odo range. The truck fired right up in the auction lot and the engine sounds wonderful with I believe little to no blow by.
A friend escorted me with a boatload of recovery tools, of which only 1.5 gallons of water was needed to top off the radiator. Why 1.5 gallons? I think the water pump is weeping as it was flickering lightly off the belt at idle. Anyway, the front end is a little floaty, when turning the wheel right it takes too much or not enough vague effort that doesn't track well, but turning left is fine. My friend escorted me 60 miles back home. It was mostly uneventful. 3 miles out I was having a little bit of fun rolling coal, and the drive belt let go. I muscled it to the front of my house with no power brakes, no power steering, no alternator charging, and no water pump turning. It didnt overheat best I can tell. Here it sits in my front yard, ready for a full assessment.
Sigh.
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I wanted more towing capacity, I have also been focusing on learning diesel engines for the past 9 months and threw myself straight in, starting with a Kubota tractor. The Silverado I currently have is the non HD 2500 with a max gvwr of 8600lbs. My next project might well be another Silverado Duramax, Powerstroke, or a 8000 lb piece of equipment. We shall see.That's a shame why get rid of it if it still works .